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Topic: TFI module going on a permanent lunch break?-SOLVED (Read 2093 times) previous topic - next topic

TFI module going on a permanent lunch break?-SOLVED

Hey guys, for a few weeks now I have been having a problem with the 'Bird(HO conversion).  Usually when it's cold, it will backfire slightly/misfire on other cylinders.  I had AR133 plugs in it which I knew were too cold for this time of year, so I swapped the Autolite 25's back in.  That helped but the problem still lingered, usually between 1500-2000rpm and approximately 20% throttle opening.  I pulled the dist. cap off and noticed the rotor was cracked...new cap+rotor and a throttle body service later and it was running like new...for about an hour.  So, I figured my wires were the next step..they were about 2yrs old and quite britle.  The problem went away all together.  About 300miles later it's back in action and worse than ever.

If I go full throttle from a dead stand still, it won't backfire or anything but just feels like it's tied to a tree until 3500rpm(like a 4cyl with nitrous...lol), it takes off like hell from there but now at about 4200-4600 it starts breaking up badly.  It's definitely not valve float...And it doesn't exhibit these symtoms ALL the time...it happens often but isn't speed or temperature specific...I'm having a hard time diagnosing it simply because there really is no patterned failures.

Any experienced advice would be welcomed

Thanks and Merry Christmas,
Don
Project 3G: Grandpa Grocery Getter-'85 Crown Vic LTD 2-door, 351W with heavily ported/polished GT40 heads, heavily ported/polished Typhoon Power Plus upper & lower intake, Comp Cams 265DEH retarded 1*, FAST EZ-EFI, HD T5, 8.8" 3.73 trac lock with extra clutches, 3G alt. swap, '99 CVPI front brakes, '09 CVPI rear disc brakes, '00 CVPI booster&m/c + wilwood adj prop valve.

Parted & Gone-'88 T-bird Sport, 351W swap, ported GT40 heads

TFI module going on a permanent lunch break?-SOLVED

Reply #1
hey sick, whats the specs on the engine, size, type of asperation, etc?

TFI module going on a permanent lunch break?-SOLVED

Reply #2
It's an internally stock '91 HO motor, no power adders.  It almost seems like it's not getting enough voltage to the ignition...like an MSD 6 getting only 11 volts...lol.
Project 3G: Grandpa Grocery Getter-'85 Crown Vic LTD 2-door, 351W with heavily ported/polished GT40 heads, heavily ported/polished Typhoon Power Plus upper & lower intake, Comp Cams 265DEH retarded 1*, FAST EZ-EFI, HD T5, 8.8" 3.73 trac lock with extra clutches, 3G alt. swap, '99 CVPI front brakes, '09 CVPI rear disc brakes, '00 CVPI booster&m/c + wilwood adj prop valve.

Parted & Gone-'88 T-bird Sport, 351W swap, ported GT40 heads

TFI module going on a permanent lunch break?-SOLVED

Reply #3
any engine codes?

TFI module going on a permanent lunch break?-SOLVED

Reply #4
Any codes?
Long live the 4-eyes!  - '83 Tbird Turbo - '85 Marquis LTS - '86 LTD Wagon-  '81 Granada GL 2dr

TFI module going on a permanent lunch break?-SOLVED

Reply #5
Sounds like a bad coil or a connection at the coil. Somewhat like a surging problem, right?

James

TFI module going on a permanent lunch break?-SOLVED

Reply #6
but also the tfi could be at fault too. but im not 100% on that.
2001 Buick Regal LS (DD):hick:

Got that fox rash again!

-Resident smartass! :ies:

- Don't listen to the naysayers. For every person who actually helps with your project there will be 10 who will discourage you all the while thinking that they are helping. 99% of all people have good intentions. That doesn't make them right.- XR7 Dave - SCCOA.Com

TFI module going on a permanent lunch break?-SOLVED

Reply #7
i never had a tfi kinda go bad, im one of the lucly ones that my mustang died in an intersection, could be a coil, try changing your fuel filter to and maybe checking the fuel pressure

TFI module going on a permanent lunch break?-SOLVED

Reply #8
I did the fuel filter a few months ago, the fuel pressure is fine(I have a rail mounted pressure gauge) and I just replaced the coil last night...didn't do any good.  The car has always had a little idle surge to it.  Friday I might try doing the TFI module and the pick-up coil inside the distributor.  I already checked the distributor shaft for excessive play, but it was tight.

On the way home from work tonight it ran like  until I was about 2minutes from home...I was at a light and stomped on it when it went green(was expecting to accelerate at a 3.8L's pace) and ended up getting wheels, so I stayed on it and barked the tires going into 2nd gear.  I don't understand it.  I'm also thinking the EEC relay could be a part of the problem...well the wiring/connections anyway.  I'll have to try to locate that just to see if the wiring is good and the connector isn't corroded or anything.

I know this has to be electrical.  I just want to find it the right way rather than the "Dart-board Diagnostics" way.

Thanks Again,
Don
Project 3G: Grandpa Grocery Getter-'85 Crown Vic LTD 2-door, 351W with heavily ported/polished GT40 heads, heavily ported/polished Typhoon Power Plus upper & lower intake, Comp Cams 265DEH retarded 1*, FAST EZ-EFI, HD T5, 8.8" 3.73 trac lock with extra clutches, 3G alt. swap, '99 CVPI front brakes, '09 CVPI rear disc brakes, '00 CVPI booster&m/c + wilwood adj prop valve.

Parted & Gone-'88 T-bird Sport, 351W swap, ported GT40 heads

TFI module going on a permanent lunch break?-SOLVED

Reply #9
Quote from: Sick88Tbird
I know this has to be electrical.  I just want to find it the right way rather than the "Dart-board Diagnostics" way.

Thanks Again,
Don


Have you run codes ????

TFI module going on a permanent lunch break?-SOLVED

Reply #10
hello,

  I had the EXACT same problem with my '89 GT that I have with a 331. When I first got it running everything was cool until a month went by. To get to the chase It ran like , bucked, stalled, poor power, ghost check engine light etc. But, also only some times. What I ended up doing was on EVERY engine connector I used ford di-electric grease. On the two big cylinder electrical plugs by the throttle body. I used fine grit sand paper and made little rolls and sanded all of the male connectors, then used the grease. I took of the TFI module and put new grease behind that and of course on the connector. I'm not joking, after that it was a totally different animal. I would say that 95% of the problems have yet to return. Give it a try!  Good luck
Only in America do we use the word "politics" to describe the process so well: "POLI" in latin meaning "many", "TICS" meaning "bloodsucking creatures".

 

TFI module going on a permanent lunch break?-SOLVED

Reply #11
I just pulled codes tonight.  KOER tests, came up with a 33 and a 92.  The 33 has to do with the EGR position sensor showing little or no activity...I'll have to clean my EGR and see what happens.  The 92 is showing that the left bank O2 sensor is sending a signal over .5 volts all the time...that's showing super fat rich...but it's not running rich anywhere.  The O2 sensor is only like 2 or 3 yrs old but I'll have to check on that also.

On the way home from work tonight, it ran like the usual  for about 5mins...the rest of the 15min ride, it was running like a raped ape.  Seems like it's getting better...knock on wood.  Now I was running colder AR133 plugs until just recently...they dont' work out too well in cold weather...I guess it's possible that they caused the O2 sensor to foul.  I plan on disconnecting the battery to clear the codes...drive it to work tomorrow and check the codes again.  I'll post back tomorrow night to let you know my results.
Project 3G: Grandpa Grocery Getter-'85 Crown Vic LTD 2-door, 351W with heavily ported/polished GT40 heads, heavily ported/polished Typhoon Power Plus upper & lower intake, Comp Cams 265DEH retarded 1*, FAST EZ-EFI, HD T5, 8.8" 3.73 trac lock with extra clutches, 3G alt. swap, '99 CVPI front brakes, '09 CVPI rear disc brakes, '00 CVPI booster&m/c + wilwood adj prop valve.

Parted & Gone-'88 T-bird Sport, 351W swap, ported GT40 heads

TFI module going on a permanent lunch break?-SOLVED

Reply #12
Okay, didn't get a chance to do anything I said I was going to...ed rain.  From my understanding, over filling the gas tank can cause the charcoal canister to fill with liquid fuel...thus causing the code 92.  Which almost makes sense being as they always crank an extra dollar worth of gas into my tank after it stops...even though I tell them not to...that and my problem started right after I filled up there for the first time.  I don't know...too many variables.  The weather should be decent tomorrow...so I'll check my O2 sensor...check my EGR and EVP sensor, the EGR vacuum solenoid as well as the charcoal canister and purge valve...hopefully I come up with something.

-Don
Project 3G: Grandpa Grocery Getter-'85 Crown Vic LTD 2-door, 351W with heavily ported/polished GT40 heads, heavily ported/polished Typhoon Power Plus upper & lower intake, Comp Cams 265DEH retarded 1*, FAST EZ-EFI, HD T5, 8.8" 3.73 trac lock with extra clutches, 3G alt. swap, '99 CVPI front brakes, '09 CVPI rear disc brakes, '00 CVPI booster&m/c + wilwood adj prop valve.

Parted & Gone-'88 T-bird Sport, 351W swap, ported GT40 heads

TFI module going on a permanent lunch break?-SOLVED

Reply #13
Well, I replaced the oxygen sensor in the left bank today...runs great below 4000rpm now.  I also removed my EGR valve only to find little balls of carbon all stacked up on the EGR valve pintle.  I replaced that valve with a significantly cleaner one and the problem is still there.  I drove it up to work and pulled the codes again, this time a 44 and a 34.  The 44 has to do with the thermactor bull...I kind of expect to see that code, being as I have the smog system gutted.  The 34 was showing as low EGR flow and/or EVP out of range...according to the manual, if I plugged the EGR vacuum supply hose and ran the test again and still got a code 34, that it was most likely the vacuum solenoid...as luck would have it, the code 34 came back.  I will pick up the solenoid tomorrow and hopefully have it on tomorrow or Sunday, weather permitting.  I'll keep  you guys posted.

Thanks,
Don
Project 3G: Grandpa Grocery Getter-'85 Crown Vic LTD 2-door, 351W with heavily ported/polished GT40 heads, heavily ported/polished Typhoon Power Plus upper & lower intake, Comp Cams 265DEH retarded 1*, FAST EZ-EFI, HD T5, 8.8" 3.73 trac lock with extra clutches, 3G alt. swap, '99 CVPI front brakes, '09 CVPI rear disc brakes, '00 CVPI booster&m/c + wilwood adj prop valve.

Parted & Gone-'88 T-bird Sport, 351W swap, ported GT40 heads

TFI module going on a permanent lunch break?-SOLVED

Reply #14
Well, it's still breaking up a little bit even after replacing the EGR vacuum control solenoid.  I want to know why the hell all those vacuum lines run behind the fender...that just seems silly to me...is there a vacuum canister there or something?  My next step is to test the EVP sensor(although I'm not so sure that's the cause). 

When free-revving, after I let off, at around 4500rpm or so, the tach will jump around just for a millisecond...that's what still leads me to believe it's the pick-up coil or tfi module...being as that's what does the primary side switching of the coil.  I guess I'll have to start testing .  It would be nice if it wasn't raining so  much.
Project 3G: Grandpa Grocery Getter-'85 Crown Vic LTD 2-door, 351W with heavily ported/polished GT40 heads, heavily ported/polished Typhoon Power Plus upper & lower intake, Comp Cams 265DEH retarded 1*, FAST EZ-EFI, HD T5, 8.8" 3.73 trac lock with extra clutches, 3G alt. swap, '99 CVPI front brakes, '09 CVPI rear disc brakes, '00 CVPI booster&m/c + wilwood adj prop valve.

Parted & Gone-'88 T-bird Sport, 351W swap, ported GT40 heads