Re: Work In Progress. '88 TC
Reply #94 –
Sunday evening I took the car to a cruise as a kind of test run. I had the spring and ball removed from the boost control valve to limit boost, but I showed some self control to keep it under 5psi. This was a test run for Tuesday with the household being down a vehicle. Found a coolant leak where the hose clamp was slipping on the new hose on the bottom. Also tighten the exhaust connection to the turbo outlet elbow.
Tuesday morning, replace hose clamp and drive the car to work. Forgot how much I actually like driving this car. Made it to and from work below 5 psi......until that last long straight before home....lean on it a little to roughly over 10 psi. No pops of intercooler piping.
Tuesday Evening, pick my son up from school a few towns away. A little more comfortable but still keep the boost pressure below 5 psi until that last straight again. Stopped and let the car eat with my son giggling the whole way with me rowing through the gears..
Saw 15 psi max through the gears......should have stopped at 10 psi without the ball and spring in the boost controller. Also, the gauge didn't climb very steady.
I am going to setup an air regulator on the wastegate actuator to watch it's function. Also think I should do a vacuum leak smoke test.
The saga continues.